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KMID : 0372919950160040543
Journal of Biomedical Engineering Research
1995 Volume.16 No. 4 p.543 ~ p.554
A Study on the Improvement of Driving Stability for the Motorized Manual Wheelchair INMEL-VII



Abstract
This paper describes the improvement of driving stability and the control system for INMEL-VII which is motorized manual wheelchair to satisfy requirements of the disabled The INMEL-VI was based on high maneuverability of the omnidirection drive and safety But the results of field tests about two years showed some problems to the disabled in daily life such as driving stability, Pm switching noise, and rotation of motor without driving command on negative slope. To solve the problems due to an increased DC motor power and applied to direct connection method in INMEL- W[, It improved the driving circuits and set switching frequency to 5KHz to eliminate the switching noise caused by PWM control of DC motor, As compare with the INMEL-VI, INMEL-VII is improved in driving stability by transfer the weight center to forward. The results of field testing proved the improvement of the driving stability and software algorithm It has been estimated to have a hlgh practical use for powered walking aids to the disabled¡¯¡¯¡¯¡¯s daily life.
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